Hi Folks- Bad Morning on the Fitchburg Line this morning (Friday 6/28). Shortly after Train 408, powered by F40 1000 came into the Fitchburg Station from the layover yard, the crankcase button blew. Of course, this rendered the train inoperable.
MBCR dispatch directed Train 410 to pick up 408's passengers. There was a delay as they were unsure whether they would couple onto to the disabled 408's set and run double draft to Boston or just proceed as a stand alone consist. It was decided to leave 408 at the Fitchburg station without coupling on and head East. There was also a delay as 410's consist had trouble contacted Pan Am's District 3 Dispatcher to obtain a Rule 241 and proceed into the Fitchburg Station Area. They eventually contacted them on the Pan Am "Yard Channel 86/86" as opposed to the "Road Channel." Passengers boarded 410 at the easternmost end of the Fitchburg Train Station platform, near Gallagher Interlocking.
At the same time, an extra was dispatched from Boston to South Acton to pick up people closer to Boston.
By the time we were moving, 410 was almost on Train 412's schedule (7:20 departure from Fitchburg). When we arrived at West Concord at 7:58, dispatch instructed the crew that they were to wait until 8:03 AM and then assume 412's schedule and make every local stop into Boston. We did, and arrived at North Station at 8:54.
I wonder what caused #1000 F40's "crankcase button" to pop. The engineer and conductor were talking and saying that it is a big "no-no" to reset it as the crankshaft could have seized thereby causing the button to "pop". I wonder if the #1000 is going to be sidelined for good if the crankshaft did break.
Like most delays, the MBCR crew did a good job of keeping everyone informed and most people took the delay in stride. Most of the North Side crews are very friendly- distinctly different of what I used to encounter when I commuted on NJ Transit.
-Mike
Last edited by mdamico23 on Fri Jun 28, 2013 11:14 am, edited 1 time in total.