by Jersey_Mike
I just got a hold of the CTEC report that details the incident. According to the timeline the train broke down at 6:22 with a non-recoverable MBC trip and at 6:30 MARC was informed and a rescue diesel was ordered from Washington. A technician was placed on MARC train 440 at 6:50 and dropped off at 6:57 and rescue diesel #63 arrived at 7:15 to couple to the stalled train. Coupling operations were complete and crews placed at both ends of the train by 7:40, but at 7:49 the train reported that it was having brake line air pressure problems and they would need to transfer passengers to train 442. By 8:41 all but 100 of the passengers were able to get on 442 and at 8:47 442 was on the move. Train 538 finally gets moving at 9:15 and arrives at NCR at 9:21 to discharge then return south to DC.
Given that the rescue diesel was ordered at 6:30 it's fairly clear that even tho it took 70 minutes to get that unit out and coupled up that was probably the best MARC/Amtrak could do with the available crews. Given today's budget situation there just isn't a lot of money to support a "hot failover" capacity. Coupling was complicated by the need to get foul time on the adjacent track #2 which by that point was clogged with rush hour trains in both directions. The obvious question is why didn't #63 take over HEP duties from the failed 4911 and at least restore A/C to the train cars and if it did perhaps the reports of being stuck for 2 hours in a hot train are exaggerated. The brake problems once the rescue locomotive was coupled were the real killer and caused a typical brakedown situation to morph into a disaster.
FYI the Amtrak CEO just sent out a company wide employee notice apologizing for the failure and calling for an increased commitment to customer service by all employees especially when it comes to communication and meeting passenger's needs in contingency situations.
Given that the rescue diesel was ordered at 6:30 it's fairly clear that even tho it took 70 minutes to get that unit out and coupled up that was probably the best MARC/Amtrak could do with the available crews. Given today's budget situation there just isn't a lot of money to support a "hot failover" capacity. Coupling was complicated by the need to get foul time on the adjacent track #2 which by that point was clogged with rush hour trains in both directions. The obvious question is why didn't #63 take over HEP duties from the failed 4911 and at least restore A/C to the train cars and if it did perhaps the reports of being stuck for 2 hours in a hot train are exaggerated. The brake problems once the rescue locomotive was coupled were the real killer and caused a typical brakedown situation to morph into a disaster.
FYI the Amtrak CEO just sent out a company wide employee notice apologizing for the failure and calling for an increased commitment to customer service by all employees especially when it comes to communication and meeting passenger's needs in contingency situations.