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  • 1970 Freight train derailment in Riverhead

  • Discussion of the past and present operations of the Long Island Rail Road.
Discussion of the past and present operations of the Long Island Rail Road.

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 #1465980  by PW team track
 
I have a photo of of 2 RS1's that were involved in a derailment. The photo only says "Riverhead 1970". The lead unit #466 is damaged on the engineers side. I am assuming it tipped on its side and the photo was taken after it was righted? Does anyone have any details on this derailment? Thank you.
 #1466087  by 4behind2
 
This may be the incident where Riverhead was evacuated due to the propane car overturning as seen in the photo. I believe there is a Daily News or Newsday article about this.

If this is the same incident, Danny Boyle was the Engr. and the late Bob McGuire was one of the Brakemen. Cannot recall the rest of the crew.
Last edited by 4behind2 on Thu Mar 22, 2018 10:18 am, edited 1 time in total.
 #1466198  by northpit
 
FrankAndCindy wrote:Hello everyone, I remember the incident when it happened. I think the conductor was diaz. They made a drop of the tank car which went wrong. A BAD MOVE> I think it was in the sixties. Thanks Frank and cindy.
can you elaborate on "A BAD MOVE" thanks north and pit
 #1466222  by jayrmli
 
The story I always heard from a retired LIRR engineer is the crew attempted to do a flying switch which didn't go as intended. (Dropping hazmat cars is a no-no to begin with.) There was a subsequent evacuation and obviously numerous emergency personnel were on the scene. Upon investigation of the scene, there were numerous beer cans strewn throughout the locomotive and caboose.

The crew was taken out of service in the incident and one of the charges was a Rule G violation. Of course, this was back in the day before strict testing and breathalizer tests.

The next day, the Long Island Press had a long story on the incident, including volunteer firefighters on site. One of the pictures in the newspaper showed one of the firefighters drinking a beer in the background. This picture was used as a defense by the freight crew, claiming that the beer did not belong to the crew, but rather the firemen. The crew wound up being reinstated.

Different times back then.
 #1466392  by LIRRcustoms.com
 
This may answer a lot of questions:

https://www.dropbox.com/s/uvb2oxhhmne9h ... h.pdf?dl=0

It is a decision of two cases regarding the aforementioned incident. The crew performed a drop or flying switch where the engines are on the facing point end of a switch and are unable to shove the cars into the siding. The engineer will accelerate his engines and the entire train before reaching the switch, bunch the slack, the conductor will pull the pin, engineer will again accelerate past the switch points while a ground man lines the switch for the diverging route after the engines pass over the switch. The cars, now uncoupled from the engines, will roll into the siding at which point a brakeman will tie on a hand brake to stop the cars in the appropriate location.

In this incident, the Engineer recalls seeing a backup sign from the ground man after his engines cleared the switch, so he reversed direction and subsequently collided with the NATX 34440 tanker which eventually exploded, destroying one engine and seriously damaging the other. A container found in the cab which was analyzed by Suffolk PD was found to have a substance which amounted to 7% alcohol by volume. It could not be proven whether this was window washing fluid or an intoxicant used by the crew, so it was eventually discounted. One empty beer can was found in the lead unit and two unopened containers of beer were found in the trailing unit's icebox. All beer cans were not found to be damaged by fire so the crew's defense was that those containers were placed there well after the fire was extinguished, possibly by firemen. It was concluded that performing the flying switch wasn't the cause of the accident but rather the Engineer mistaking a hand signal by a ground man to reverse direction before the entire consist cleared the main track.

I won't post the crew member's names in this thread, but you can see the names of all parties involved in the link above. The outcomes of the two investigations are also listed. The PDF file above was found and saved from the National Mediation Board's website at http://www.nmb.gov/.